2021-2023 Repairs: Apache 37 Rudder, Anchor Windlass,  Cabin Top

Fuel Polishing and  Diesel Tank Cleaning

Rudder Repair

In 2021 my buddy Dave and I were sailing to Maine, when he noticed that there was a tiny bit of play in the tiller. The rudder and tiller have always been super tight. Now it had maybe 1/4" to 1/2" of motion at the end of the 3' tiller, certainly not much. I checked the tiller, tiller hinge, and top rudder bearing and they were all fine.  But on a 53 year-old rudder, play in the rudder itself could be bad. I didn't know exactly how the rudder was constructed internally, but I suspected stainless plates, welded to the rudder stock (shaft). Then surrounded by wood. Is the wood badly rotten? Worse, if there are lets say 3 plates welded to the shaft, maybe 2 of the welded plates had broken loose? Time to investigate.

First step: Where is the play?

There is less than 1/8" of the rudder shaft visible above the rudder when it is mounted to the boat. I wanted to get a large pliers on the shaft. I dropped the rudder about 3/4", enough to get a vise-grip on the shaft, and sure enough, the play was between the shaft and the rudder. Not good.

Second: Remove rudder and bring it home. Easy enough. I removed the rudder in the fall so I could troubleshoot it properly over the winter.

Third: I got a small metal detector. The metal detector showed thin metal parts fore-and-aft, about 1/4 and 1/2 way from the top. It showed  one larger metal area near the bottom. I drilled 1/4" holes. The 'rods' were about 1/2" wide, in the center of the rudder (about 1" deep) and the plate was very close to the surface. It was close to the surface on both sides. Strange, definitely not conventional rudder construction. The core is solid mahogany. The wood was in good condition. A bit of moisture, but all solid. 

With a grinder, a chisel, and reciprocating tool I opened up the areas around the joints between the shaft and the rods, and between the shaft and the plate.

openings

The rods are 3/8"  and go through holes in the 1.5" shaft. The ends of the rods are peened over to keep them from moving. The bottom plate is maybe 3/16: stainless or Monel, and is bent (wrapped) around the the shaft. All of these had a bit of play. Apparently the rods or holes in the shaft have worn and loosened up a bit over 53 years of sailing. 

The good news is that the play probably wouldn't get too much worse and should not fail catastrophically. The bad news is that it will gradually get a bit worse over time, and all the rudder torque depends on these 2 rods. The shaft is constantly moving in the rudder, making it almost impossible to keep water out of where the shaft enters the rudder, top and bottom. This could help explain some of the winter cracking that I have experienced the past 7 or so years. After thinking about it for a while, I decided to have the rods and plate welded to the shaft, and to add some small stainless gussets welded on to strengthen the joints on both sides. This worked very well. My thanks to Lawton welding in Topsfield, MA. They do stainless welding very well.
weld1

bot
        weld
Here is the process of glassing up the holes. I filled the larger voids with chunks of foam core, ground the area down, then added 2-3 layers of biaxial stitch mat (1708).
        closed

Faired everything, added 3 layers of barrier coat, and installed it. The top of the rudder is very close to the skeg, like 1/16".

installed

BTW, here is a disturbing image of a more 'standard' Apache 37 rudder that failed in 2021. You can see the 3 plates that I expected, with the bottom one broken off, and the resulting rudder gone.

BSrudder 

Cabin top sides Delam

I had patched up and painted the port cabin side to repair a few feet of delam, maybe 2-3 inches wide, just under the opening ports. I painted the cabin sides over the repair. 15 years later, it was apparent that my patch wasn't holding. There were cracks and blisters in a strip almost 10' long. Also the two large ports were leaking, so this would be a good time to remove and rebed them.

In the fall of 2021, we hauled early, in mid-September, for a hurricane that never happened. I took advantage of the nice autumn weather to do this long-awaited project. I stripped the 15 year old paint, removed the two large ports, glassed the gap between the outer skin and the headliner,  and ground down about a 10' strip where the delam was. I added some glass, ground and faired it, and tried to match the gel-coat color. I don't have good before and after photos, just this one 'after' example of poor color matched gel-coat. The two ports are the large ones. Not sure why the photo is upside-down.

cabin side

The reapair went well. Gelcoat color match is still not perfect, but at least it is smooth, structurally sound and weatherproof. The starboard side needs a similar repair, but much smaller.

2020 New Roller Furler

My roller furler was an ancient Cruising Design continuous line unit. It used an internal wire halyard and required a temporary halyard to be fitted to raise or lower the sail. It was not convenient to change sails, and so we rarely did it. One of the extrusions had some serious longitudinal cracks, and the furling line regularly jumped the drum. It was time.

My original small jib was original 1968 vintage. It had been damaged and I rarely used it. I tried to get a new small jib made in 2017, but my favorite sailmaker was too busy. So I took the measurements to Ebay, and found a great North Genoa from a 35'-ish boat. The UV cover was my color, Captains Navy, and it had the perfect sail number: 42! The price was right at $500. We put it on, thinking we would use our 135% when the wind was light. That was 5 years ago and we have never changed it once. As we get older and are more conservative sailors, being underpowered is more desirable than being overpowered. I single-hand a fair amount too. Whenever the thought enters my mind "Maybe we should change to the big jib" the wind picks up shortly after. We love our small jib. We almost never need to reef the jib.

We looked at Harken furlers, and finally were convinced by Kevin at Northeast Rigging to use the smaller (Size 1, up to 36') racing version (MKIV). Going smaller saved $ and weight, and considering that we regularly use a small jib and so rarely reef, it has worked very well.

2022 Anchor Windlass

As I age, hoisting our 35# anchor and 45' chain also gets old. We purchased a new Maxwell Windlass and installed it on our Summer 2022 Maine Trip. Happy, Happy, Joy, Joy.

I use a teak fairing block to raise the windlass up a bit since the chain needs to go up over the bullwark which is nearly 6" high. The vertical angle is limited to about +/- 6 degrees.

windlass
Here is the rope to chain splice in process.
splice

Inside the chain locker. I had some problems with the rope binding when raising anchor. Originally I thought it was that the chain drop wasn't enough: it needs to be 12". I removed the windlass and examined the hole. I use a riser block and the holes in the riser block and the deck didn't line up perfectly, so the rope was sticking on the block. I enlarged the block hole to line up with the deck hole, smoothed the holes, and all is well.

locker
And the anchor. I needed to swap the plow from port to starboard since the windlass chain is on the starboard side.
anchor


2023 Bottom Stripping

I have been wanting to strip the bottom for years. The old bottom paint is thick and hard, and sometimes comes off in chunks. The bottom is not smooth. I tried a few times to strip parts of the bottom. I tried scraping, sanding, and chemical strippers. It is a messy and back-breaking job. In addition my boat yard discourages bottom stripping. I do very small areas and keep the mess cleaned up at all times.
I saw some reviews, and decided to try a small area of stripper called Peel-Away last Fall using their gallon size. It only did about 20 sq ft.
I bought a 5 gallon pail of it ($180) and did the aft, port quarter this past spring. It  easily removed the top layers. I tried a second application and it helped, but the old hard bottom paint is really tough. Instead I scraped it with a two-handed carbide scraper. Tough work, I did a bit at a time. Eventually I built up my upper-body muscles and we able to do 15-30 minutes of scraping at a time. I did a bit each day until it was all down to bare gelcoat. Then a final sanding and applied 3 layers of Interlux 2000 barrier coat.

I figure I'll do 1/4 of the hull each year. About 1/5 of it was already done.

bot
These long scrape marks are not mine, they were there under the red paint.

bot
You can see some of the red paint here. The stripper took off many layers of blue, but the red needed to be scraped.

bot
After sanding and a couple of coats of Interlux barrier coat. Ahhhhh.

2023 Fuel Polishing, Tank Cleaning

After launching in May 2023, we were motoring to the mooring for the first time of the season. The engine slowed and died, acting like fuel lines or filter was plugged. The sight glass on the bottom of the Racor didn't look too bad. I have a vacuum gauge to tell me when the filter is clogged, and it read 0 as it always does meaning no clog. I replaced the filter element and found a bunch of crud in the filter housing. I checked the vacuum gauge and it was broken, stuck at 0! A few days later we went for the first sail of the season. We motored away from the  mooring just fine, sailed for 2 hours, then started the engine to motor back to the mooring. The engine slowed and died. We sailed back to the mooring. Sailing had stirred up the tank and plugged the fuel line. .

This identical scenario had occurred in 2014, 9 years ago. At the time I built a simple fuel cleaning system using a small electric fuel pump and some cheap plastic fuel filters. The Racor housing and the fuel lines were badly plugged with diesel bug. I cleaned the filter, lines and the tank. No problem since then.

I fired up the old electric fuel pump and it did not work. I contacted a local fuel polisher, but the logistics didn't work. He needed me to be at a dock with AC power, but the docks he suggested were unavailable. And I may have had to tow the boat to the dock. Time to DIY it again, and do it right this time. And time to be more preventative about this problem in the future.

I bought another cheap ($80) auto-parts-store fuel pump and some small filters. These filters quickly plugged so I had to back-flush them several times. But they got most of the major crud.

Also access to my tank is difficult as the fuel gauge port is about 8" under the cockpit. I could only access it while lying in the starboard quarter-berth.  Last time, I think I drained most of the tank, removed all the fittings, loosened the straps, and and tilted the circular tank to starboard about 30 degrees, to make accessing the port easier. Ugh. This time I cut a 6" hole in the cockpit sole just above the tank. I made a simple 1/8" aluminum cover. This made accessing the tank so much easier.

I investigated better fuel pumps and filters, and found what I think is an ideal combination. The small parts-store or Amazon electric fuel pumps are low capacity and don't prime well. The ones intended for fuel transfer are high capacity (10 gal / min) and can overwhelm a filter. Tractor Supply has pumps made by Remco, Fimco and others, and intended for chemical spraying including oil based fertilizers. They are about 2-4 gal / min and about $100. I bought the Remco 3300 and it worked very well.

For a filter, you need a large one to handle 2 gal/min. I found a Racor 900 Chinese clone on Amazon for just $52. Perfect! 30 micron filter elements are about $13. Not sure I would use a cheap clone filter permanently on my boat, but for this once-a-year fuel-polishing job, it seemed ideal. I used 3/8" flexible sprayer hose, also from Tractor Supply. Worked well.

I mounted the pump, filter, and a switch to some scrap plywood, and use a 3/8" OD bend-able copper tube in the tank. It reaches all the nooks and crannies. I used an inspection camera to inspect the dry parts of the tank to check for diesel bug. 

hole
Here is the 6" hole I cut in the cockpit sole. Got to love that Apache 37 foam-core deck layup. I plan to recess the aluminum cover a bit. Spring boatyard project.

polish

So if you have an old boat with an old diesel tank, here are my recommendations:

Here is the crud that this tank cleaning session dredged up, about 12oz in a 24oz jar.Pretty nasty.

nasty